Signed-off-by: Steven Robertson <steven@strobe.cc>
Reviewed-by: Paul B Mahol <onemda@gmail.com>
Signed-off-by: Michael Niedermayer <michael@niedermayer.cc>
For the 10-show-existing-frame, the source file indeed has a timestamp
of 3 (or 100/33) for the second visible frame, so the fix appears to
work correctly. For the other, only the timebase is fixed, but again
appears to be correct now.
This fixes a fate failure after bumping the minor version
Its unknown why this is not needed for the other aac tests,
more investigation needed but for now i dont want to leave
it broken while its investigated
Signed-off-by: Michael Niedermayer <michael@niedermayer.cc>
There were some errors in the calculation as well as an entire
unnecessary loop to find the gain coefficient. Merge the
two loops.
Thanks to @ubitux for the suggestions and testing.
The fate test command line is supposed to serve as an example. It's
nicer to explicitly state the profile rather than setting options
to force it for you.
GCC 3.4 miscompiles it on sunos. Date of release? The second of
August two thousand and five, anno Domini. That's ten years two
months and fourteen days ago. Three thousand seven hundred and
twenty seven days ago. One sixth of the average life expectancy
of a person living in a country with a human development index
of zero point eight hundred and eight, equality adjusted.
GCC 4.3 also miscompiles it, though not as bad.
The LTP encoding and the test is a bit slow currently, taking twice
the amount of time the other tests do, so in the future the
total time to encode might be cut down on that test.
These aren't quite as helpful as the ones in 8bpp, since over there,
we can use pmulhrsw, but here the coefficients have too many bits to
be able to take advantage of pmulhrsw. However, we can still skip
cols for which all coefs are 0, and instead just zero the input data
for the row itx. This helps a few % on overall decoding speed.
It was useful to (accidentally?) spot an overflow in the column pass
of the x86 simple_idct10 implementation.
Signed-off-by: Michael Niedermayer <michael@niedermayer.cc>
omse goes from 0.03060703 (which fails for dct-test) to 0.01663750.
This also actually improve the error of decoding the sample generated
by fate-vsynth3-dnxhd1080i-10bit using simple_idct10 to FAANI, which
goes (when resampled to yuv422p) from:
stddev: 0.06 PSNR: 72.28 MAXDIFF: 1
to identical.
Signed-off-by: Michael Niedermayer <michael@niedermayer.cc>
Includes escapes that should now be supported and a few features not yet
fully supported, like comments, regions, classes, ruby, and lang.
All were tested with https://quuz.org/webvtt/ for validation, except
regions because the validator doesn't support them yet, and I couldn't
find any other way to validate WebVTT.
Signed-off-by: Ricardo Constantino <wiiaboo@gmail.com>
It was merged with the iff_ilbm decoder in commit
929a24efff.
Define AV_CODEC_ID_IFF_BYTERUN1 as AV_CODEC_ID_IFF_ILBM for API
compatibility.
Reviewed-by: Ronald S. Bultje <rsbultje@gmail.com>
Signed-off-by: Andreas Cadhalpun <Andreas.Cadhalpun@googlemail.com>
This finalizes merging of the work in the patches in ticket #2686.
Improvements to twoloop and RC logic are extensive.
The non-exhaustive list of twoloop improvments includes:
- Tweaks to distortion limits on the RD optimization phase of twoloop
- Deeper search in twoloop
- PNS information marking to let twoloop decide when to use it
(turned out having the decision made separately wasn't working)
- Tonal band detection and priorization
- Better band energy conservation rules
- Strict hole avoidance
For rate control:
- Use psymodel's bit allocation to allow proper use of the bit
reservoir. Don't work against the bit reservoir by moving lambda
in the opposite direction when psymodel decides to allocate more/less
bits to a frame.
- Retry the encode if the effective rate lies outside a reasonable
margin of psymodel's allocation or the selected ABR.
- Log average lambda at the end. Useful info for everyone, but especially
for tuning of the various encoder constants that relate to lambda
feedback.
Psy:
- Do not apply lowpass with a FIR filter, instead just let the coder
zero bands above the cutoff. The FIR filter induces group delay,
and while zeroing bands causes ripple, it's lost in the quantization
noise.
- Experimental VBR bit allocation code
- Tweak automatic lowpass filter threshold to maximize audio bandwidth
at all bitrates while still providing acceptable, stable quality.
I/S:
- Phase decision fixes. Unrelated to #2686, but the bugs only surfaced
when the merge was finalized. Measure I/S band energy accounting for
phase, and prevent I/S and M/S from being applied both.
PNS:
- Avoid marking short bands with PNS when they're part of a window
group in which there's a large variation of energy from one window
to the next. PNS can't preserve those and the effect is extremely
noticeable.
M/S:
- Implement BMLD protection similar to the specified in
ISO-IEC/13818:7-2003, Appendix C Section 6.1. Since M/S decision
doesn't conform to section 6.1, a different method had to be
implemented, but should provide equivalent protection.
- Move the decision logic closer to the method specified in
ISO-IEC/13818:7-2003, Appendix C Section 6.1. Specifically,
make sure M/S needs less bits than dual stereo.
- Don't apply M/S in bands that are using I/S
Now, this of course needed adjustments in the compare targets and
fuzz factors of the AAC encoder's fate tests, but if wondering why
the targets go up (more distortion), consider the previous coder
was using too many bits on LF content (far more than required by
psy), and thus those signals will now be more distorted, not less.
The extra distortion isn't audible though, I carried extensive
ABX testing to make sure.
A very similar patch was also extensively tested by Kamendo2 in
the context of #2686.
Currently only 2 profiles are evaluated because they are the only 2
with distributed test sequences.
- CID 1260: YUV 4:2:2 10 bits with block-adaptive interlace coding,
from ticket 4876;
- CID 1270: YUV 4:4:4 10 bits (HR), 1920x839, from ticket 4581.
They were generated from the ticket sequences by running the
following kind of command-line;
ffmpeg -i $INPUT -an -sn -vcodec copy -vframes 1 -y $OUTPUT.mov
Signed-off-by: Michael Niedermayer <michael@niedermayer.cc>
The current one, while correct, does not yield the best possible
results. The specificiations suggest another formula, which results
in quality gains in the decoded output from fate tests. This
justifies changing said formula.
Signed-off-by: Michael Niedermayer <michael@niedermayer.cc>
Convert them to zigzag order, as the rest of them are.
When I was adding support for 10-bit DNxHD, I just copy-pasted the
missing quant matrices from the spec. Now it turns out the existing
matrices in dnxhddata.c were in zigzag order. This resulted in wrong
quantization for 10-bit DNxHD. The attached patch fixes the problem by
converting 10-bit quant matrices to zigzag order.
Signed-off-by: Michael Niedermayer <michaelni@gmx.at>